Pollution Prevention and Control Technologies for Plating
Operations
Section 3 - Chemical Recovery
3.4 ION EXCHANGE
3.4.6 Performance Experience
3.4.6.1 Nickel Plating Performance Experience
3.4.6.2 Chromium Plating Performance Experience
3.4.6.3 Non-Cyanide Zinc Plating Performance Experience
3.4.6.4 Cadmium Cyanide Plating Performance Experience
3.4.6.5 Gold Cyanide Plating Performance Experience
3.4.6 Performance Experience
A summary of the Users Survey data for ion exchange recovery applications
is presented in Exhibit 3-31. Within this exhibit, the response
data has been grouped by types of plating solution. These include:
nickel, chromium, non-cyanide zinc, cadmium cyanide, and gold
cyanide. A general discussion of the ion exchange data is presented,
followed by specific information regarding each of the different
types of applications.
The following information and data summarizes the performance
experience of the survey respondents.
- The average satisfaction level for ion exchange recovery is
3.2 (on a scale of 1 to 5, with 5 being most satisfactory), which
is lower than the average level rating for chemical recovery in
general (weighted average for all chemical recovery applications
is 3.4). Fifty-four percent of the shops indicated that this technology
satisfied the need for which it was purchased and another 11%
indicated that it partially satisfied their need. Thirty-five
percent indicated that it did not satisfy the need for which it
was purchased. The following is a breakdown of the reasons why
shops purchased this technology (not all shops responded and some
shops gave multiple reasons):
To meet or help meet effluent regulations:.........21
To reduce plating chemical purchases:...............8
(includes all four gold applications)
To reduce the quantity of waste shipped off-site:..14
To reduce wastewater treatment costs:..............13
To improve product quantity:........................6
Other:..............................................0
- The use of ion exchange generally did not impact production
quality or the rate of production. The following responses were
provided:
Product Quality Production Rate
Improved 5 1
No Change 16 18
Decreased 3 4
- The majority of plating shops indicated, that based on their
experience with this technology, if given the chance they would
purchase the same type of equipment from the same vendor. The
following is a breakdown of their responses:
Purchase the same technology from the same vendor:.... 18
Purchase the same technology from a different vendor:...0
Purchase a different technology:........................8
Do nothing:.............................................2
The major savings from the operation of ion exchange for non-gold
applications was due to reduced water use and reduced sludge generation.
For gold applications, the major savings was due to the recovered
gold.
3.4.6.1 Nickel Plating Performance Experience
Thirteen respondents to the User Survey provided detailed data
regarding their experience applying ion exchange to nickel rinse
waters. Two of these responses cover systems that were being installed
at the time of the survey and therefore, no performance data are
available from these shops (PS 105, PS 139). Three shops used
the process for a short time period, but abandoned their efforts
due to disappointing results (PS 212, PS 317, PS 318). None of
the remaining eight shops currently operate the traditional recovery
configurations (Exhibit 3-22), where the cation regenerant is
subsequently processed by electrowinning to recover the nickel
or nickel sulfate is returned to the bath. At one time, PS 124
recycled nickel sulfate regenerant directly to the bath. However,
this shop discontinued use of the process due to "continuous
and repeated" equipment failure. PS 015 purchased an electrowinning
unit for nickel recovery, but the unit did not work and therefore,
they selected to treat the regenerant instead. Also, one of the
two new installations plans to operate with metal recovery (PS
139). Three shops use off-site recycling for regeneration of their
columns (PS 161, PS 196 and PS 063) and another shop regenerates
on-site and sends the regenerant to an off-site metals recycling
firm (Inmetco) (PS 261).
Although no on-site recovery is presently practiced, the configurations
used by the respondents involve the recycle of water. These applications
have been included in this recovery section because they process
a segregated nickel rinse water with ion exchange. As such, that
they most likely experienced many of the same performance and
O&M problems as recovery operations.
The following performance details were provided by survey respondents:
- The two most successful installations among survey respondents
are PS 161 and PS 261. PS 161 sends their used ion exchange columns
to off-site services for regeneration, most recently using Dayton
Water Systems for regeneration of both nickel and chromium columns.
This shop has used this form of off-site recycling since 1972.
Originally, their equipment was purchased from Pollutronics and
the columns were regenerated in Cleveland (company name not specified).
They used Culligan's service in the late 1970's until 1991, when
they switched to Dayton Water Systems "because of their recycling
ability." After contacting Dayton Water Systems, it was learned
that they do not currently provide a regeneration service for
heavy metals, but may resume this service in the near future.
The ion exchange columns used by PS 161 contain 3.2 ft3 of mixed
(anion and cation) resin. During the past year, PS 161 sent 18
nickel columns and 8 chromium columns to Dayton Water Systems.
The cost of the service was $336 per column for regeneration plus
a $70 per month rental fee for the equipment (therefore, the total
annual cost for most recent year is $6,888 for nickel and $3,528
for chromium). According to PS 161, Dayton Water Systems sent
the regenerant to Inmetco for recovery of the metal (see Section
7 for information on off-site recycling).
- Only one of the shops indicated that an ion exchange unit
applied to nickel plating was the cause of an effluent compliance
excursion (PS 196). This shop stated: "Excursions happen
when the mixed bed of resin is saturated with copper and nickel
and will no longer polish the water." This shop uses an off-site
service for regeneration and is charged by the number of columns
used. Therefore, the shop may tend to load the resin beds to their
maximum or beyond their breakthrough point.
- PS 261 reported a satisfaction level of 4 for ion exchange
applied to nickel rinse waters. Their configuration is unusual
in that the ion exchange unit is connected to the first rinse
tank (i.e., most concentrated). Rinse water from the first rinse
is pumped through the ion exchange column and is recycled to the
last rinse (four-stage counterflow system). With this configuration,
the ion exchange column receives the most concentrated rinse water.
The normal configuration (see Exhibit 3-22) makes use of drag-out
recovery to reduce the chemical load on the ion exchange system
and recycles the final rinse. Using their configuration, PS 261
probably experiences the need for frequent regeneration. Their
regenerant is sent to Inmetco for off-site recycle.
- PS 317 and PS 318 applied ion exchange to rinse waters from
electroless nickel plating. Both shops eventually abandoned their
efforts to make the technology work. PS 317 described their use
of the technology as a poor experience and indicated that their
unit "required more water to restore the resin beads than
water being processed." PS 318 indicated that the "process
did not meet expectations or effluent guidelines."
3.4.6.2 Chromium Plating Performance Experience
Five respondents to the Users Survey provided some detailed data
on their experience using ion exchange for chromium recovery.
One of these shops uses an off-site regeneration/recycle service
(PS 161) for regenerating columns applied to decorative chromium
rinses (chromic acid, fluoride, barium carbonate). This shop also
uses the off-site service for nickel recovery, details of which
are provided in Section 3.4.6.1. Another respondent (PS 305) regenerates
their unit on-site and sends the regenerant (sodium dichromate)
to an off-site recycle company (Inmetco). One of the respondents
recovers chromium from combined chromic acid anodizing and chromate
conversion coating rinse waters and recycles the anion regenerant
(dichromate) to the dichromate seal tank (PS 001). This system
includes both anion and cation columns. The cation column removes
contaminants such as aluminum and the anion column removes hexavalent
chromium. Rinse water from the first rinse is filtered and passes
through the columns and is returned to the final rinse. The cation
column regenerant is treated and the anion column regenerant is
transferred to the dichromate tank. Two of the four respondent's
systems are not currently in use, but were previously used for
chromium recovery from hard chrome plating rinse waters. One of
these respondents intends to put their system back into use if
the need arises (PS 052). Presently they have zero discharge,
which is achieved through drag-out recovery rinsing. Bath contaminants
are removed using membrane electrolysis and a porous pot. The
other shop tried the ion exchange process for a short time period
in 1984 and does not intend to reuse it in the future (PS 080).
The following information and data summarize the performance experience
of the five survey respondents.
- In one case, performance was hampered by operational and maintenance
problems. PS 080 indicated that: "Initial attempts to use
ion exchange for removal of impurities from chromic acid rinse
water failed. Resins became fouled and could not be regenerated
and maintain plating production throughput requirements."
It should be noted that this system was relatively inexpensive
($3,025) as compared to the other chromium recovery units. The
respondent indicated that the supplier stated capacity was 200
gpd and that the actual capacity was 0 gpd. The respondent provided
a diagram in the survey that seems to indicate they were processing
rinse water from drag-out tanks. This solution may have been overly
concentrated with chromic acid for the apparently small ion exchange
unit, causing almost immediate total loading of the resin. Also,
their low capital expenditure may indicate that prefiltration
was not included with the purchased ion exchange equipment.
- PS 001 indicated that the supplier stated capacity and the
actual capacity of their ion exchange system was 6 gpm at a feed
concentration of 100 mg/l CrO4. At this flow rate the system recovered
98% of the chromium.
- None of the shops indicated that an ion exchange unit applied
to chromium recovery was the cause of an effluent compliance excursion.
3.4.6.3 Non-Cyanide Zinc Performance Experience
Five respondents to the Users Survey provided data on their experience
with ion exchange used with non-cyanide zinc plating. Only two
of these respondents provided sufficient detail to be considered
useful for this report (PS 061 and PS 130). Both of these systems
were manufactured by the same company and were purchased just
one month apart. One ion exchange system was applied to acid zinc
and the other to alkaline zinc. As will be discussed, the performance
of the two systems was reportedly very different. The more successful
of the two systems (PS 130) is a combination ion exchange and
electrowinning system, similar in configuration to that shown
in Exhibit 3-22. The other shop (PS 061) used ion exchange as
an end-of-pipe treatment for "zinc bearing rinses and selected
bath dumps," with the ion exchange regenerant going to an
evaporator for concentration and the concentrated solution being
hauled to an off-site recycle firm. The ion exchange processed
wastewater was pH adjusted and discharged to a city sewer. This
shop does not have a conventional hydroxide precipitation system
following the ion exchange process. Originally this shop planned
to return the zinc chloride concentrate from the evaporator to
the zinc plating tank. As discussed later in this section, this
plan did not work.
The following information and data summarize the performance experience
of the two survey respondents.
- One of the two shops providing detailed data on zinc applications
indicated that their ion exchange unit was not the cause of an
effluent compliance excursion (PS 130). The other shop indicated
that their overall treatment system, which included zinc and chromium
ion exchange, evaporation and pH adjustment, caused an effluent
limitation excursion. Their treatment system was put into operation
in December, 1989. On July 4, 1990, they received a cease and
desist order from their control authority.
- The performance of the ion exchange system operated by PS
061 was hampered by operational and maintenance problems. These
are discussed in Section 3.4.6.3.2. The supplier stated capacity
of this application was 18 gpm and the actual capacity was 10
to 12 gpm.
- PS 061 originally planned to recover the zinc chloride regenerant
by concentrating it with evaporation and then reusing it in the
zinc plating tank. This was not possible due to: (1) Chromium
was present in the regenerant, and to remove the chromium would
have required redesigning the ion exchange system. (2) The amount
of zinc chloride generated by "false regenerations (a constant
problem)" was much more volume than could be used in the
plating tank, even after evaporation. (3) The low pH of the regenerant
kept destroying the heaters in the evaporation unit and the steam
from the system was so acidic that it corroded a hole in the shop
roof. This shop also tried to recover the zinc using electrowinning.
They found that it was too difficult to maintain a chemical balance
during the process and that chlorine gas was liberated. Both problems
made the process ineffective and the electrowinning unit was never
put into full operation.
- Although PS 130 gave their system a satisfaction level rating
of 3, they indicated that its downtime due to O&M problems
was 50%.
- Both of the shops indicated, that based on their experience
with this technology, they would purchase a different technology
if given the opportunity to repeat the process.
3.4.6.4 Cadmium Cyanide Performance Experience
Four respondents indicated that they have used ion exchange for
chemical recovery with a cyanide plating solution other than gold
cyanide. These four shops included four applications to cadmium
cyanide rinse waters and one for zinc cyanide rinse waters (one
shop did both).
The shop using both applications (PS 229) installed their equipment
in stages during the early to mid-1980's and it was integrated
with an HSA electrolytic recovery system. The shop provided insufficient
details to draw any conclusions, however, they offered the following
as a summary of their experience with the combined system: "Costs
in 11 years far outweigh benefits. Would have been much more practical
to install conventional precipitation technology."
The other three respondents also provided sketchy information
for their applications. One of the units was a pilot system purchased
in 1991 that is still being used in 1993 (PS 025). The response
from that shop indicate that they are relatively satisfied with
the system. PS 245 used a rented ion exchange column for cadmium
recovery and found that the resins "loaded very quickly and
did not appear to be the right application." They intend
to use the equipment following conventional precipitation for
water reuse. Since these two applications require different types
of resins, it appears that this respondent has not received sufficient
technical support to utilize this technology. PS 254 purchased
ion exchange equipment in 1985 for cadmium recovery. They later
eliminated the ion exchange process because it was recycling ferrocyanides
to the plating bath.
The following information and data summarizes the performance
experience of the survey respondents.
- The major savings from the operation of ion exchange for this
application was the result of water use reduction, treatment chemical
reduction and sludge volume reduction.
- PS 229 reported that the capacities of their ion exchange
columns were 50 percent of the supplier stated capacity (2 lb/column
vs 4 lb/column). They also indicated that they were unable to
reuse either their zinc chloride or cadmium chloride regenerant
due to an excess volume problem in the plating tank (i.e., insufficient
surface evaporation from the low temperature baths). They evaporate
water from the zinc chloride regenerant (500 gpy) and send the
concentrated solution to a landfill. They electrowin cadmium from
that regenerant (1,000 gpy) and then send the metal-depleted regenerant
to off-site disposal. A discussion of cyanide plating applications
is presented in Section 3.4.3. Low cation capacity may be due
to excess free cyanide. Methods for concentrating the solution
and making headroom in the plating tank using evaporation are
discussed in Sections 3.2 and 3.3. Electrowinning of the cadmium
regenerant is an acceptable method of recovery. The recovered
metal can often be used as anode material. It is possible to increase
the recovery rate by reusing the cation regenerant following electrowinning
(see Exhibit 3-22). PS 229 also indicated that the fact that their
equipment manufacturer went out of business within two years of
installing their ion exchange equipment hindered the performance
of their application.
- None of the shops completing the survey indicated that an
ion exchange unit applied to cyanide plating rinse waters was
the cause of an effluent compliance excursion.
3.4.6.5 Gold Cyanide Performance Experience
Five user survey respondents provided some detailed data on their
experience with ion exchange used for gold recovery. All but one
of these shops send their used resins to their gold solution suppler
for credit toward bath chemicals. The other shop regenerates the
resin on-site and uses electrowinning to recover the metal (PS
123). The following information and data summarizes the performance
experience of the survey respondents.
- The average satisfaction level for ion exchange applied to
gold cyanide is 4.0 (on a scale of 1 to 5, with 5 being most satisfactory),
which is higher than the average level rating for ion exchange
chemical recovery in general. Also, all of the shops indicated
that this technology satisfied the need for which it was purchased.
In each case the need was identified as reducing plating chemical
purchases or other (i.e., reclaim gold). The range of savings
from gold recovery for these shops was $1,320 (PS 283) to $134,400
(PS 123) per year.
- Only one of the shops provided any capacity data. PS 179 indicated
that they experience an average resin loading of 4 troy ounces
per cubic foot of resin. They typically use 1 ft3 of resin per
year.
- In some cases, performance was hampered by operational and
maintenance problems. These are discussed in Section 3.4.7.
Next Section|Main Table of Contents|Section 3